Thought I'd update this old thread with a quick teardown report 2 years later.
I've got 93 runs on the motor, about the equivalent of 7+ gal. of fuel.
All looks good, started to get some increased end play in the front bearing so I changed them both. Also had 66 runs on the rod needles and found they had worn about 0.0001" (a tenth) and were dark so replaced them too. Interesting the crank pin hasn't worn at all that I can measure.
Piston fit is still good, there was some slight deto on the exhaust side, also on the head, cleaned them up easily with some 400 grit.
There was minor galling on the crank where it seals just before the front bearing, cleaned it off with 400 grit paper.
It's completely stock, head set at 0.012", 60% nitro with 12% oil (1/3rd castor).