I believe John Finch bumped the Gas Sport Hydro record over 84+ mph. (3mph increase)Just checkin to see if anyone here has any info on how the SAW gang is doing in NC today.Thanks!!
OK, a motor that qualifies as "sport".A stock os ,wright.
Yup, the boating gods did not smile on me for sure. After much discussion with John and Steve over dinner Saturday night (while we were still sober ) we pretty much figured out the sequence of events of the crash. First attempt with a new set of props resulted in a very bad hopping condition so I brought the boat right in and went back to the props that I set the record with last fall. On the second outing John tossed the twin in to the left, I brought it around & cracked the throttles once going left to right down the back straight & the boat jumped right up so at that point I had decided to make one blast right to left to make sure it tracked well & then come in and shorten the pipes. Came around & lit 'er up, the boat was singing sweet and came through the traps at what I was told by Mr. Sutton after the crash just a tick under 107. From that point we figured the rudder blade failed just past the second timing light (the top half of the blade was still there, even the 4-40 shear bolt was intact with no signs of stressing whatsoever) which lifted the back as it tore off causing the right sponson tip to dig in shearing it off immediately, snapping the boat to the left and to the shoreline where it ultimately came to rest. Judging by the amount of wood that was still floating in the water after I picked the carcass up off the shore most of the damage occurred when it snap rolled left ripping off the sponson & rear shoes, flattening both strut blades over & sending both fuel tanks out through the bottom of the tub. It was not a pretty sight when it was over but it happened so fast you didn't even have time to say "OH S---!!!" For those who e-mailed & pm'd me wanting to know what went wrong it just took me a day to "get over it" and post what happened. I will rebuild the boat this winter to go at it again as I know beyond a doubt there is still a bunch more speed in it & we will go alot faster in '09. Even though it was a heartbreaker for sure the fact of being around a bunch of good people sure took the sting out of it. Nothing like friends and some alcohol later that evening to make one feel a little better. B)Don Ferrette lit off the twin hoping to up his record. His second attempt was disasterous he hit a turtle or a stick or his rudder broke, the twin left the water and landed on the shore. That was a bad sound when he hit the shore!!
Hey,The OB's were definetly on their game this weekend.The 20 OB hydro record was smashed with a stock OS. Pretty cool.
Yes it did. make me another one just like it! I will need a back up in Huntsville in two weeks. I may squeeze out 74 or 75 mph with it there because I was running full water and never pulled a plug when i made the 71.4 mph pass.Carl,
It looks like that propeller matched up rather well with the O.S. motor.
Glad you had success this past weekend in NC. 70.66 MPH WOW!!!
Thanks For The Business Carl,
Mark Sholund
Joe,Carl, Do you have any pics of your o/b outrigger? I sure would like to see this boat. Thanks, Joe
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